Thread Rating:
  • 0 Vote(s) - 0 Average
  • 1
  • 2
  • 3
  • 4
  • 5
Diagnosing Hydraulic Failure in the CAT 345 Excavator
#1
The CAT 345 and Its Hydraulic Architecture
The Caterpillar 345 hydraulic excavator is a heavy-duty machine designed for large-scale earthmoving, demolition, and quarry operations. Introduced in the early 2000s, the 345 series features a robust hydraulic system powered by dual variable-displacement piston pumps, electronically controlled through the AEC (Automatic Engine Control) and MCV (Main Control Valve). With an operating weight exceeding 90,000 lbs and breakout forces over 60,000 lbs, the 345 became a staple in high-production fleets across North America and Asia.
Its hydraulic system is designed to prioritize efficiency and responsiveness, using pilot-operated valves and load-sensing circuits to modulate flow based on demand. However, when components like the MCV, pilot relief valves, or pump control circuits fail, the machine can become sluggish, unresponsive, or even stall under load.
Symptoms of Hydraulic Dysfunction and Engine Stall
In one documented case, a CAT 345 with serial number AGS01473 experienced severe hydraulic degradation. After rebuilding the MCV and replacing both joysticks, the machine still suffered from slow or nonexistent hydraulic response. When the AEC was active, hydraulic output dropped significantly. Eventually, the machine began stalling when attempting to travel, even at full RPM.
Observed symptoms included:
  • Hydraulic functions only activating when two joysticks were engaged simultaneously
  • Travel motors attempting to engage but stalling the engine before movement
  • Implement pilot pressure measured at only 325 psi at full throttle
  • No movement from travel levers despite engine effort
Terminology:
  • MCV (Main Control Valve): The central hydraulic valve block that distributes flow to implements and travel motors
  • AEC (Automatic Engine Control): A system that adjusts engine RPM based on hydraulic demand
  • Pilot pressure: Low-pressure hydraulic signal used to actuate main valves and release travel brakes
  • NFC (Negative Flow Control): A feedback system that adjusts pump output based on valve demand
Root Causes and Diagnostic Pathways
When hydraulic functions fail and the engine stalls under load, the issue often lies in the pump control logic or pilot pressure circuit. In this case, the pilot pressure was far below the expected 400–500 psi range, which is necessary to release travel brakes and activate implement valves. A weak spring in the pilot relief valve or incorrect valve rebuild could be responsible.
Potential root causes:
  • Misrouted NFC signal lines between left and right pumps
  • Weak or misadjusted pilot relief spring
  • Faulty pump control solenoids or sensors
  • Internal leakage within the MCV or travel circuit
  • Swivel joint bypass or seal failure (common in older 330 models)
In one similar case involving a CAT 330, resealing the swivel joint restored travel function. However, in the 345, the issue persisted, suggesting a deeper problem in the pilot circuit or pump control logic.
Testing and Adjustment Recommendations
To isolate the fault, technicians should:
  • Measure pilot pressure at the MCV pilot relief port at various RPMs
  • Verify NFC signal routing and ensure left/right pump lines are not reversed
  • Inspect pump control solenoids for voltage and response
  • Adjust pilot relief spring tension to achieve 400–450 psi
  • Check travel brake release pressure and confirm valve actuation
If pilot pressure remains low, replacing or rebuilding the pilot relief valve may be necessary. In one field repair, adjusting the spring tension resolved sluggish hydraulics and restored travel function.
Lessons from Field Experience
Experienced technicians emphasize the importance of understanding hydraulic interdependencies. When one function fails, it can cascade through the system. For example, low pilot pressure not only prevents travel but also disables implement valves, leading to misleading symptoms. Engaging two joysticks may temporarily increase demand and trigger partial flow, but this is not a sustainable fix.
In Ontario, a technician diagnosed a similar issue by observing engine stall behavior and confirming that the pump was over-demanding due to incorrect control signals. By tracing the NFC lines and correcting their routing, full hydraulic function was restored without replacing the pump.
Conclusion
Hydraulic failure in the CAT 345 excavator often stems from pilot pressure loss, misrouted control signals, or faulty valve rebuilds. When the machine stalls under load and hydraulic functions become erratic, technicians must methodically test pilot circuits, pump controls, and valve logic. With proper diagnosis and adjustment, even severe symptoms can be resolved without major component replacement. In machines like the 345, hydraulic precision is everything—and when the system falters, it’s not just about flow, but about knowing where the signal breaks down.
We sell 3 types:
1. Brand-new excavators.
2. Refurbished excavators for rental business, in bulk.
3. Excavators sold by original owners
https://www.facebook.com/ExcavatorSalesman
https://www.youtube.com/@ExcavatorSalesman
Whatsapp/Line: +66989793448 Wechat: waji8243
Reply


Possibly Related Threads…
Thread Author Replies Views Last Post
  CAT 302.5 Mini Excavator: Troubleshooting Common Issues MikePhua 0 1 7 minutes ago
Last Post: MikePhua
  Diagnosing and Resolving Fuel Priming Issues in the Case 590SM Backhoe MikePhua 0 1 12 minutes ago
Last Post: MikePhua
  Diagnosing and Adjusting Track Tension on Caterpillar Track Loaders MikePhua 0 1 12 minutes ago
Last Post: MikePhua
  Diagnosing and Resolving Air Ingress in Diesel Fuel Systems MikePhua 0 1 14 minutes ago
Last Post: MikePhua
  Case 888 Wheel Loader: Diagnosing and Repairing Hydraulic Pump Leaks MikePhua 0 1 16 minutes ago
Last Post: MikePhua
  Replacing the Hydraulic Line from Filter to Pump on a Bobcat 773 Skid Steer MikePhua 0 1 18 minutes ago
Last Post: MikePhua
  Solenoid Valve Failure on a Hitachi 490E and Hydraulic System Diagnostics MikePhua 0 1 19 minutes ago
Last Post: MikePhua
  Restoring the Swivel Post on a Warner Swasey Hopco 550 Excavator MikePhua 0 1 20 minutes ago
Last Post: MikePhua
  Takeuchi TB135 Mini Excavator: Troubleshooting and Repair Insights MikePhua 0 1 21 minutes ago
Last Post: MikePhua
  Fuel Contamination in Coolant: Diagnosing and Resolving Issues in the Caterpillar 3126 Engine MikePhua 0 3 22 minutes ago
Last Post: MikePhua
  Diagnosing Drive Motor Misalignment and Frame Damage on the Bobcat 864 Track Loader MikePhua 0 3 25 minutes ago
Last Post: MikePhua
  Komatsu PC200 Excavator Glow Plug Relay Location and Troubleshooting MikePhua 0 1 35 minutes ago
Last Post: MikePhua
  Diagnosing Overheating in the CAT D6B Dozer with the D333A Engine MikePhua 0 1 36 minutes ago
Last Post: MikePhua
  Auxiliary Hydraulic Line Pressure Relief in Excavators MikePhua 0 1 36 minutes ago
Last Post: MikePhua
  Komatsu PC200 Excavator Glow Plug Relay Location MikePhua 0 1 38 minutes ago
Last Post: MikePhua

Forum Jump:


Users browsing this thread: 1 Guest(s)