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Troubleshooting a Non-Functional Fuel Gauge on the Bobcat 863 Skid Steer
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Bobcat 863 Overview and Electrical System Basics
The Bobcat 863 was introduced in the late 1990s as a mid-frame skid steer loader powered by a turbocharged Kubota V2203 diesel engine. Known for its hydraulic performance and reliability, the 863 featured a simple analog dashboard with gauges for fuel, temperature, and system voltage. The fuel gauge system consists of a float-type sending unit inside the tank, a two-wire harness, and a dash-mounted analog meter. While mechanically straightforward, age and vibration often lead to electrical faults that disable the gauge.
Terminology Note
  • Fuel Sending Unit: A float-based sensor inside the tank that varies resistance based on fuel level.
  • Gauge Circuit: The electrical path from the sending unit to the dashboard meter.
  • Ground Reference: A stable electrical return path required for accurate gauge readings.
  • Open Circuit: A break in the wiring that prevents current flow.
  • Short to Ground: A fault where a wire contacts metal, bypassing the intended circuit.
Symptoms and Initial Observations
A newly acquired Bobcat 863 had a history of fuel leakage, traced to a damaged grommet on the tank. The previous owner replaced the grommet and installed a new fuel level float assembly. Despite this, the fuel gauge remained non-functional. The gauge itself was reportedly tested and confirmed operational, and the sending unit was new. The issue appeared to be electrical, likely within the wiring harness or connector interface.
Diagnostic Strategy and Wiring Checks
To isolate the fault, follow these steps:
  • Inspect the wiring harness from the sending unit to the dashboard. Look for pinched, frayed, or corroded wires.
  • Use a multimeter to measure resistance across the sending unit terminals. A full tank should read low resistance (~10 ohms), while an empty tank should read high (~90 ohms).
  • Check for continuity between the sending unit and the gauge input pin.
  • Verify ground integrity by measuring resistance between the sending unit ground and chassis ground.
  • Test the gauge by grounding its signal wire—if the needle moves to full, the gauge is functional.
In Missouri, a technician found that a Bobcat 863 had a broken wire inside the loom near the firewall. The wire had corroded internally, showing continuity at rest but failing under vibration. Replacing the harness resolved the issue.
Common Faults and Solutions
  • Loose connector pins at the tank or dashboard—tighten or replace terminals.
  • Incorrect float orientation—ensure the float arm moves freely and is not obstructed.
  • Missing ground strap—install a dedicated ground wire from the sending unit to the frame.
  • Aftermarket sending unit mismatch—verify resistance range matches OEM specs.
  • Dashboard gauge failure—swap with a known-good unit to confirm.
Recommendations for Long-Term Reliability
  • Use dielectric grease on all connectors to prevent corrosion.
  • Secure wiring with loom and clamps to reduce vibration fatigue.
  • Replace grommets and seals with OEM-grade rubber to prevent fuel vapor intrusion.
  • Keep a wiring diagram on hand for future troubleshooting—many are available through Bobcat dealer networks or service manuals.
Conclusion
A non-functional fuel gauge on the Bobcat 863 is often caused by wiring faults, grounding issues, or mismatched components. Even with a new sending unit and confirmed gauge, the circuit must be tested thoroughly for continuity and resistance. With proper diagnostics and attention to harness integrity, the fuel gauge can be restored—ensuring accurate readings and preventing unexpected shutdowns due to low fuel.
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